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As it seems I'm having to pull the differential center sections more that I
like due to axle and now locker damage. I built a new tool to place on
my floor jack to allow me to easily pull and re-install them. this
sure beats the attempts with a transmission jack, or my normal way of just
man handling it in and out. - February 2016 |



















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For those who wheeled last November at the Badlands in Attica Indiana, you
remember in addition to discovering my ARB locker was broken, I also had a
fuel injection problem. I've fixed the ARB, and it should be as good as
new. I started the wiring change to be sure the computer was feed clean full
voltage and install the solid state relays. Well, I found a couple of issues
that I believe were causing my problems. The system ground wire
connection at the engine intake had come loose. Also the ignition feed wire
to the power relay had a bad crimp (not one I made). So what I first thought
was a bad relay (I'd swapped it out before the trip) and the computer shut
downs at the Bad Lands turns out to be both a ground and power connection
issue! Now I need to put the dash back together and then move to the
engine bay and install the new high volume water pump to address the high
rpm overheating issue. However the small radiator leak will likely be a more
difficult problem to fix as the good radiator shop here in Decatur went out
of business. - March 2016 |
















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Well, I think I've found my High RPM cooling issue on my (Modified) M37.
This issue has been going on for a while and back in March of 2014 I had a
small radiator leak and pulled it to have it fixed and cleaned as I thought
that was the issue. Well it wasn't. So I figured it must be the water
pump. I ordered a High-Performance GMB Short Snout Water Pump to replace and
upgrade the M. Well the old pump is just fine. The new pump has an improved
water channel path design, but has a slightly smaller impeller (4-3/8" Old &
4-1/16" New) so I hope the new pump isn't a down grade. I knew it wasn't
a lower hose issue as it had a good hose and internal spring. The issue was
at highway speeds, or high RPM's off roading so I was looking for a coolant
flow or capacity issue. The radiator has developed another small leak, so it
came out again and will get re-cleaned to be sure it has good flow. Back
after I built the engine in 2005 and got the M on the road in 2007 I had a
thermostat leak. I pulled the thermostat out and found the aftermarket
aluminum housing was not flat, so I filled it flat and cleaned everything up
and resealed it with no leaks. The thermostat looked good and was new in
2005. The thermostat was a Robertshaw 180º part number 370-180. This type of
thermostat has a lower cup that opens downward opening up around the outer
edge between the thermostat and the intake. As the thermostat was the
only thing left, I pulled it out again. I found two issues: Some of the
sealant had oozed into the space between the side of the thermostat lower
cup and the intake. Also when I placed the thermostat in water, it only
started opening up at 190º and at boiling it was only open about 1/8". So
between a poorly operating thermostat and a partially obstructed path, I
think (hope) that is my cooling issue. It was just not able to push enough
coolant across the radiator under high heat loads. So I have a new Napa
Premium Thermostat on order. So I'm keeping my fingers crossed that this
cures the issue, and will get it back together as soon as I get the radiator
repaired. - April 2016 |
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After I put the dash all back together after making the electronic
updates/fixes to address the EFI problems, I tore into the coolant issues.
Had the leaks (17 of them) fixed in the Radiator (A to Z Radiator in
Springfield IL) and installed a couple of side shields before re-installing
it, the new water pump and thermostat. I poured in the coolant in and
nothing ran back out, however when I started the engine, the thermostat
housing was spitting coolant out both sides frown emoticon . Originally I
when I built the engine the new aluminum housing would not seal, and I found
it wasn't smooth and flat. So back then I pulled it out and filed it smooth
and flat, but added plenty of sealant. The sealant stopped the leak, but
excess was likely causing part of my overheating problem as it was
interfering with the Robershaw thermostat. So even though I properly cleaned
and re-filled the housing, I only applied a light amount of sealant, thus
the leak. So off it came another cleaning and a more liberal application of
sealant. Thankfully no more leaks, but the engine still runs about 210º
at 3,000 RPM at 60 MPH down the road. Cooler than before but still not as
cool as I'd like. I'm running a 180º thermostat. I'm guessing the engine
just generates more heat then the radiator (new core in 2005) can handle.
Could be a gauge issue, I did check the engine with an IR unit and it looked
to be 10º cooler than the gauge read. - April 2016 |
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